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Low-load Efficiency Improvement of a Three-Phase Bidirectional Isolated DC-DC Converter (3P-BIDC) Via Enhanced Switching Strategy
Author(s) -
Nuraina Syahira Mohd Sharifuddin,
N. M. L. Tana,
Hirofumi Akagi
Publication year - 2018
Publication title -
international journal of engineering and technology
Language(s) - English
Resource type - Journals
ISSN - 2227-524X
DOI - 10.14419/ijet.v7i4.35.28297
Subject(s) - modulation (music) , burst mode (computing) , switching frequency , phase (matter) , mode (computer interface) , three phase , control theory (sociology) , electronic engineering , computer science , materials science , voltage , engineering , electrical engineering , physics , control (management) , acoustics , quantum mechanics , artificial intelligence , operating system
This paper presents the system design, operation and enhanced switching strategy of a three-phase bidirectional isolated dc-dc converter (3P-BIDC). The paper discusses the operating modes of the 3P-BIDC using phase-shift modulation (PSM), with analysis on its soft-switching characteristics. The phase-shift modulation is the simplest modulation technique that can be applied to the 3P-BIDC. However, it comes with the consequences of low efficiency performance in the low-load conditions. Therefore, this paper investigates the improvement in efficiency of the 3P-BIDC during low-load condition using an enhanced switching strategy combining burst-mode switching and phase-shift modulation. The model of a 700-V, 100-kW, 20-kHz 3P-BIDC and the enhanced switching strategy are verified via simulation using PSCAD. The simulation results shows that the combination of burst-mode and phase-shift modulation technique improves the efficiency of the 3P-BIDC at low-load conditions.  

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