z-logo
open-access-imgOpen Access
Shutdown analysis and treatment of 150MW steam extraction heating unit due to low oil fuel level
Author(s) -
Wanjun Li,
Xiaoxia Li,
Qingliang Niu,
Tianqi Huang
Publication year - 2019
Publication title -
iop conference series. earth and environmental science
Language(s) - English
Resource type - Journals
eISSN - 1755-1307
pISSN - 1755-1315
DOI - 10.1088/1755-1315/300/4/042014
Subject(s) - shutdown , oil pressure , oil pump , fuel oil , petroleum engineering , automotive engineering , boiler (water heating) , environmental science , leakage (economics) , fault (geology) , turbine , waste management , engineering , nuclear engineering , mechanical engineering , economics , macroeconomics , seismology , geology
When the 150MW steam turbine generator set of a power plant operates normally, the pressure of EH oil system gradually decreases and the fuel level drops in the tank, then switching to standby EH oil pump, the pressure of EH oil system continues to drop to the protection action, and the unit shutdown. Through on-site inspection and inspection of maintenance records, it was found that there was serious oil leakage at the oil outlet of mobile oil filter and the oil outlet pipe of EH oil cooling pump. The cause of the fault was analyzed accurately. Effective measures such as changing the connection mode between mobile oil filter and EH oilto eliminate the potential safety hazards in equipment operation.

The content you want is available to Zendy users.

Already have an account? Click here to sign in.
Having issues? You can contact us here