
Application of integrated reservoir management and reservoir characterization to optimize infill drilling. Quarterly technical progress report, September 13--December 12, 1996
Publication year - 1996
Language(s) - English
Resource type - Reports
DOI - 10.2172/463572
Subject(s) - reservoir modeling , petroleum engineering , infill , reservoir engineering , drilling , reservoir simulation , geology , oil field , petroleum reservoir , engineering , civil engineering , petroleum , mechanical engineering , paleontology
Eighteen 10-acre infill wells have been drilled and completed as part of the Field Demonstration phase of the project at the North Robertson (Clearfork) Unit (NRU). The fourteen producing wells are pumped-off and producing at stable rates. The four injection wells are completed and have been on injection for three to four weeks. Current Unit production is approximately 3,400 STBO/D, of which approximately 900 STBO/D is being produced from the 10-acre infill wells. A change in the Statement of Work has been approved so that additional 10-acre infill wells can be drilled and/or 20-acre producing wells can be converted to injection during the next quarter as budget constraints and rig availability allow. Technical progress is described for the quarter in many related areas: implementation of the field demonstration; reservoir characterization; reservoir management activities and performance analysis; reservoir simulation; and technology transfer