z-logo
open-access-imgOpen Access
CHEMICAL TECHNOLOGY DIVISION, UNIT OPERATIONS SECTION MONTHLY PROGRESS REPORT FOR AUGUST 1959
Author(s) -
J.C. Bresee,
P.A. Haas,
R.W. Horton,
C.D. Watson,
M.E. Whatley
Publication year - 1959
Language(s) - English
Resource type - Reports
DOI - 10.2172/4205932
Subject(s) - coolant , chemistry , uranium oxide , heat transfer , materials science , uranium , metallurgy , thermodynamics , physics
The concentration gradients of uranyl ion in aqueous and organic solutions were analyzed by taking a macro photograph of the desired gradient by monochromatic (436 m mu ) light transmitted by the solution normal to the gradient in an appropriate diffusion cell. Two Druhm runs were terminated due to malfunction of the sodium metering system and the third run was terminated when the UF/sub 6/ nozzle ruptured. Calculations of particle temperature versus time relations for the flame denitration-calcination method of preparing metallic oxide from nitrate solutions indicate that the times required for heat transfer are controlled by the rate of radiant heat transfer to particle surfaces instead of by conductive heat transfer within the particles. A completed experimental study indicated that electrolysis in a cell with a mercury cathode and a platinum anode is a practical process for removing nickel from HRT fuel solution. The apparent diffusion coefficient of uranium loading on Dowex 21K was shown to be directly related to the resin size. An explosion of sufficient violence to blow apart the Pyrex pipe dissolver occurred during the fifth Darex dissolution of simulated SRE fuel probably from a rapid gas phase reaction between hydrogen and oxidizing gases such as NO/sub 2/. Materials handling flowsheets were completed for (A) decladding, washing, recanning and storing spent SRE uranium fuel slugs and (B) the shearing and leaching of stainless steel clad UO/sub 2/ and UO/sub 2/- ThO/sub 2/ fuels. A literature survey is being conducted dealing with reactor coolant and coolant loop contamination and decontamination. During run R-17 for calcination of evaporated Darex waste, the same as run R-16 which deformed the bottom calcination vessel except that one of the three added pressure probes was vibrated to keep it unplugged, the bottom of the calcination vessel did not deform, and there was no pressure indicated on the pressure probes during the test. (For preceding period see CF-59-7-58.) (auth

The content you want is available to Zendy users.

Already have an account? Click here to sign in.
Having issues? You can contact us here