Work Improvement at a Car Manufacturing Company
Author(s) -
Muhamad Zameri Mat Saman,
Cheak Ying Law
Publication year - 2012
Publication title -
jurnal teknologi
Language(s) - English
Resource type - Journals
eISSN - 2180-3722
pISSN - 0127-9696
DOI - 10.11113/jt.v37.523
Subject(s) - humanities , physics , computer science , art
Productivity has been identified as an important role in any organization, especially for manufacturing sectors to gain more profit that leads to prosperity (1). This paper reports a work improvement project in a car manufacturing company. It involves problem identification at the metal finish line and proposing recommendation to improve the efficiency of the current situation. Based on the observations and the collected data, online work-in-progress (WIP) has been identified as a major problem and this is caused by insufficient movements due to material handlings and unbalanced workload. Method improvement technique is used to determine the best method of carrying out a task in order to eliminate the unnecessary movements. Then, line-balancing technique is used to minimize the idle time at every station or the percentage of line balance loss (LBL). In order to verify the results that were obtained from the generated line-balancing alternatives, Witness simulation package is used to estimate the output. One effective alternative is chosen based on the results obtained from the simulation and cost justification. Then, a proper planning is suggested to maximize the resource utilization at the metal finish line. Simulation results showed that productivity increases about three times higher than the current situation. However, the results were obtained based on several assumptions that was made in the analysis. Abstrak. Produktiviti merupakan sesuatu yang amat penting bagi sesebuah organisasi, terutamanya bagi sektor pembuatan ke arah meningkatkan keuntungan untuk memajukan syarikat. Kertas kerja ini melaporkan satu kajian kes bagi pembaikan kerja di sebuah syarikat pengeluaran kereta. Kajian kes ini terbahagi kepada dua bahagian iaitu mengenalpasti masalah di lini pemasangan utama dan mencadangkan pembaikan ke arah meningkatkan kecekapan sistem yang sedia ada. Berdasarkan kepada pemerhatian dan juga data yang dipungut, kerja tergendala di lini pengeluaran adalah merupakan masalah utama. Ia disebabkan oleh sistem pengangkutan bahan yang kurang cekap dan pembahagian kerja yang tidak seimbang. Teknik pembaikan kerja digunakan untuk mencari penyelesaian yang terbaik bagi mengatasi masalah di atas. Kemudian, kaedah keseimbangan lini digunakan untuk meminimumkan masa melahu pada setiap stesen kerja. Untuk mengesahkan keputusan daripada alternatif-alternatif yang dicadangkan, simulasi dengan menggunakan perisian Witness telah digunakan. Satu alternatif terbaik dipilih berdasarkan kepada keputusan daripada simulasi dan juga justifikasi kos. Akhir sekali, perancangan sumber dijalankan ke arah memenuhi permintaan dan juga memaksimumkan penggunaan sumber.
Accelerating Research
Robert Robinson Avenue,
Oxford Science Park, Oxford
OX4 4GP, United Kingdom
Address
John Eccles HouseRobert Robinson Avenue,
Oxford Science Park, Oxford
OX4 4GP, United Kingdom